Effect of aeration and recirculation in the removal of nitrogen and chemical oxygen demand from sanitary sewage in a structured bed reactor

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Abstract

his study aimed to evaluate a structured bed reactor with intermittent aeration in the simultaneous removal of Chemical Oxygen Demand (COD) and Total Nitrogen (TN) from sanitary sewage. The reactor was operated for 339 days with a Hydraulic Retention Time (HRT) of 12 hours, temperature of 30 ± 1°C and continuous feeding. Nine trials were carried out in which three different effluent recirculation flow (Qr), 3, 2 and 1 time the incoming flow, were evaluated in three different aeration times, of 1h, 2h, and 3h, in 3 hour cycles. The results showed that different recirculation flows and aeration times did not influence the removal of COD, which reached 89%±12. It was observed that the efficiency of TN removal was higher in the tests with higher COD/TKN ratio, between 7.2 and 7.8, reaching TN effluent values of 17 mg. L-1, being 5 mg. L-1 of N-NH4+, 2 mg. L-1 of N-NO2 and 10 mg. L-1 of N-NO3-. It was verified that it is possible to remove the COD and nitrogen from sanitary sewage in a structured bed reactor with intermittent aeration.

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Leick, S. A., De Oliveira, J. G. B., Tavares, K. A., Lopes, D. D., & Barana, A. C. (2017). Effect of aeration and recirculation in the removal of nitrogen and chemical oxygen demand from sanitary sewage in a structured bed reactor. Engenharia Agricola, 37(6), 1236–1243. https://doi.org/10.1590/1809-4430-eng.agric.v37n6p1236-1243/2017

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