Energy and environmental assessment of steam management optimization in an ethylene plant

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Abstract

Steam crackers (ethylene plants) belong to the most complex industrial plants and offer significant potential for energy-saving translated into the reduction of greenhouse gas emissions. Steam export to or import from adjacent units or complexes can boost the associated financial ben-efit, but its energy and environmental impact are questionable. A study was carried out on a me-dium-capacity ethylene plant using field data to: 1. Estimate the energy savings potential achievable by optimizing internal steam management and optimizing steam export/import; 2. Quantify the associated change in air pollutant emissions; 3. Analyze the impact of the increasing carbon price on the measures adopted. Internal steam management optimization yielded steam let-down rate minimization and resulted in a 5% (87 TJ/year) reduction in steam cracker’s steam boiler fuel consumption and the associated cut of CO2 emissions by almost 4900 t/year and that of NOx emissions by more than 5 t/year. Steam import to the ethylene plant from the refinery proved to be purely economic-driven, as it increased the net fuel consumption of the ethylene plant and the refinery complex by 12 TJ/year and resulted in an increase of net emissions of nearly all considered air pol-lutants (more than 7000 t/year of CO2, over 15 t/year of NOx, over 18 t/year of SOx) except for CO, where the net change was almost zero. The effect of external emissions change due to the associated backpressure electricity production surplus (over 11 GWh/year) was too low to compensate for this increase unless fossil fuel-based electricity production was considered. The increase of carbon price impact on the internal steam management optimization economics was favorable, while a switch to steam export from the ethylene plant, instead of steam import, might be feasible if the carbon price increased to over 100 €/tCO2.

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APA

Variny, M., Hanus, K., Blahušiak, M., Furda, P., Illés, P., & Janošovský, J. (2021). Energy and environmental assessment of steam management optimization in an ethylene plant. International Journal of Environmental Research and Public Health, 18(22). https://doi.org/10.3390/ijerph182212267

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